Page 3 of the
Princess chronology
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A brochure from 1971
February 2010 and the car has been under wraps for a couple of months.
Despite the excessive cold weather it fires up OK, when I remember to pull out
the choke that is. In March I take it to Autocraft in Mexborough for checking the underseal & waxoyl protection, greasing of all joints, fixing a couple of
small paint issues and replacement of the front engine mount. Despite the
greasing, my feelings are that the CV joints are worn and will need replacement
in the near future.
08.04.2010 Since the purchase of the car, there have been
scratches evident on the driver's door glass. Today I managed to get hold of a
replacement door glass from a breakers yard at Balby, Doncaster which was fitted
at Autocraft the following day. A very fiddly job not made easier
by the design of the door - there being no removable panels.
The left rear tyre shows signs of age so is replaced using the (new) spare. The
old one is now the spare.
The following Sunday sees the first show of the year. A sunny, but chilly day
out at the Elsecar Heritage Centre in Barnsley brings out the cars and
the crowds.
31.05.2010 Many miles covered over the weekend of the
29th to the 31st of May. My first attendance at Carlton Towers near Goole/Selby
for their steam rally saw a reasonable show. However, incessant light rain (from
start to finish) dampened spirits! It also affected the car which would not
start when requested. Apparently the solenoid was stuck and was soon rectified.
Thanks to Steve Turner of the Cambridge and Oxford Owners Club. The following
day at Thornton le Dale near Pickering saw sunshine and only light showers. A
good show of Vehicles in this typical North Yorkshire village. Finally, at
Sherburn Aero Club, probably the best show so far with agreeable weather. A wide
variety of vehicles (from 1908 to the present day) and aircraft with a Spitfire
Trainer and the Battle of Britain Memorial Flight's Hurricane taking the
starring roles. No further problems with the Princess.
Sentinel DG6 steam lorry at Carlton Towers, Vintage line up at Thornton &
display at Sherburn
06.06.2010 A 60 mile trip down the
motorway to Nottingham through a thunderstorm for the Autokarna rally at
Wollaton Park ends in disaster. On leaving the motorway the car misfires and
loses power. I notice white smoke at the rear. Initial thoughts are that it has
something to do with excessive water getting in to the electrics. I crawl to the
show ground and discuss matters with other attendees and come to the conclusion
that the head gasket has blown. This is further borne out when No. 2
spark plug is cleaned and the fluid thereon is found to be pink - the same
colour as the coolant. The radiator needs topping up too. The RAC gets a call to
recover the car home and, for once, take no more than 10-15 minutes to turn up.
07.06.2010 As expected, the head gasket has failed
between No.2 & 3 cylinders. Plenty of water (coolant) spurting from these
cylinders when the engine is turned over. The cylinder head requires
attention and is sent for machining. 4 of the valve guides need replacing
and the remaining 4 are 'marginal', therefore, to replace all.
The picture shows the affected area of the gasket.
18.06.2010 The head is returned from the engineers. It
has been refaced, as was the manifold, and the valve guides replaced. New studs
were manufactured and a new copper gasket set supplied. To make it look the
part, I undertook a bit of painting to both the cylinder head and the
manifold with very high temperature enamel paint.
On initial running the engine sounds rough and is no better when taking the car
for a run, so is returned for tuning. A couple of hoses are split (fuel pipe
from the carb. & manifold breather hose) and the vacuum advance/retard mechanism
of the distributor needs replacement. These matters are temporarily fixed until
I can get the correct parts and, consequently, the engine is now running
perfectly.
It was discovered, during this time, a couple of holes in the bodywork which
will need urgent attention as water ingress is evident. Both sills are affected,
so carpets out for further investigation!
30.07.2010 The sills mentioned above are, apparently,
in good order but required cover plates on both sides. Repair also made to left
rear floor near subframe mounting. Front interior floor and boot floor
repainted.
01.08.2010 The engine sounds as though the exhaust is
blowing but am unable to find the source. This later proved to be the manifold
to front pipe joint.
15.08.2010 The wheel bearings and brake cylinders
are in poor condition and the distributor retard unit was found to be
leaking. It appears the retard unit is not the original so a closer matched unit
was purchased and fitted. All other jobs completed prior to successful MOT
on 23rd August. New CV joint boot kits fitted. To replace the front
tie rod & lower arm bushes in the near future.
Despite the amount of work done (and yet to do!) on the Princess, the 'show season' has largely been quite successful mainly due to the good weather encouraging people to bring out their vehicles. Here are just a few pictures of some of the shows attended throughout the year.
From left to right: June-An evening at 'The Baxters', Fenwick; July-1935
Lanchester at Thornes Park, Wakefield; Jowett and Bedford Campers at Newby Hall,
Ripon.
All at Newby-Ford Y&C Club, Model T Ford, 1953 David Brown Lagonda Drophead,
1937 Cord 812 Phaeton
1933 Austin 7 Box Saloon at Newby; August-Brodsworth Hall near Doncaster, 1975
Type 2 VW Camper; September-Daimler 'Empress' at Rotherham.
October-Skipton, North Yorks, Albion Coach; Commercials & Buses at Sandtoft
Trolleybus Museum near Doncaster
20.11.2010 The tie rod & lower arm bushes are replaced along with a braided fuel pipe. A stone damages the exhaust near to the silencer box and this is rectified as well.
28.01.2011 The car has been in the body shop for 8 weeks and was returned today. Hopefully, the water ingress problem (mentioned 18.06.2010) has been solved. A portion of the 'A' post was actually missing (it appears a previous repair was badly done) and required attention. Water was running down the the 'A' post where it meets the wing, getting into the sills and into the cabin. Therefore, the lower wings (both sides) and first 2 inches or so of the sills had to be repaired & repainted. The missing part of the 'A' post was replaced by welding in new metal. A couple of paint chips (on the nearside sill & inner wing) were attended to. The wing mirrors were replaced as a mark where they were previously was becoming evident (they were removed to provide a more aesthetically pleasing look!). A thorough coating of waxoyl should see the year out and with the carpets replaced the car should be ready for the road. The paint on both wings has not been matched correctly and needs to be redone.
State of nearside & offside A post to sill. Right, new metal welded in
Showing the finished article.
22.04.2011 Smashed the left front
sidelight/indicator lens - too embarrassing to say how. They are quite rare and
hard to find (and therefore expensive) and, after a few days of searching my
spirits were low. However, a Scottish contact (see Contacts
page) came up trumps and hopefully I will receive one in the next few days.
27.04.2011 New lens fitted.
04.05.2011 The paint for the wings, mentioned above,
has been matched as closely as possible. It appears the original paint used in
the respray in 2009 was not correctly matched, being too dark. The codes for
this mixture have now been recorded.
10.05.2011 The wings are repainted there is,
however, some overspray on the front bumper rail. It later transpires the area
where the wing meets the rail was poorly prepared as bubbles are appearing
beneath the paint.
21.05.2011 Oil flush, oil and filter change at 77,742
miles. Note to self - remove old seal before putting in the new!!!
July 2011 The engine sounds as though
it is not firing on all cylinders on starting, only settling down after a minute
or so.
20.08.2011 Changing the spark plugs cures the
misfire. No.2 plug is 'gunged up' - probably the reason.
At various shows during the year including; Newark, Notts; Glossop; Heath
near Wakefield; Hayfield Lakes near Doncaster; The Travellers Rest, Hope Valley;
The Moor, Sheffield.
25.09.2011
Following a visit to York, there is a strange noise coming
from the engine bay. It seems like a new dynamo is required as it is getting hot
and the exclamations coming from it are persistent.
28.09.2011 Purchased rear exhaust mountings
(bobbin type) to replaced the existing two which had a couple of splits in the
rubber. I took the opportunity to shorten the exhaust as it was
protruding beyond the rear bumper and causing a nuisance.
30.09.2011 After a lot of 'huffing & puffing', I
finally managed to replace the dynamo. There was movement around the bushes of
the old one and, as refurbishment would cost as much as a new one, it was
replaced.
06.11.2011 A run to Lincoln was the final show of the
year. The car has covered a little over 2,300 miles attending ahows this year.
04.03.2012 The car has slept in the garage
over-winter and, surprisingly, started first time. After a short run all seems
okay.
27.03.2012 Spoke too soon! On turning the ignition -
nothing but a click. As a similar problem occurred before, I assumed it was the
solenoid, but after purchasing one it turns out the starter motor is
kaput and so is sent for refurbishment. Unfortunately, it is beyond repair - a
new one ordered.
30.03.2012 It appears the new starter motor has 10
teeth on it's shaft whereas the old had 9. As the old shaft was in good order it
was fitted to the new motor. The car fires up but is
misfiring. Adjusting the position of the distributor cures the problem. As I
have found in the past, the Haynes Manual over-simplifies the removal &
refitting procedure. The manual states; disconnect cables, remove 2 bolts and
lift out, where in fact; disconnect battery earth cable, remove the grill to
gain access, remove the distributor (do not undo the distributor clamp as I did)
as the starter motor will not come out as it is blocked by this and the oil pump
housing. Disconnect the other cables, remove bolts & lift out. On refitting,
ensure the distributor is in the same position to ensure the timing is the same.
30.05.2012 Discovered some 'play' in right front wheel.
As there has, for some time, been some cracking noises on turning it was decided
to replace the diveshaft collars & nuts, right front ball joint & wheel
bearing, both track rod ends and the CV joints were swapped over. The left
front brake was binding due to a seized cylinder so this was freed up & both
brake pads renewed.
18.06.2012 The left front brake binding has returned and is
much worse.
22.06.2012 Apparently, the brake hose had become
blocked probably due to deterioration from the inside. This was cleared but
replacement hoses would be a sensible purchase.
As there had been a knocking noise emanating from the engine bay (?against the
bulkhead I thought), this was investigated and found the exhaust front pipe
catching the right side driveshaft. In an attempt to ease it away the exhaust
manifold broke at its neck. A replacement was sourced and fitted. It did not
have the breather nozzle, however, so the crankcase breather hose was re-routed
and now fits onto the air cleaner box. This, however, proved to be
unsuccessful as it appears the 'air flow' was disturbed (not enough vacuum?) and
oil was forced out of the dipstick & filler neck openings. A Mark 3 manifold was
found which had the appropriate breather nozzle plus a nozzle for a brake servo
hose. The latter was blocked off as my car has no servo. All is now back to
normal! A small hole in the exhaust back
box was welded and probably means a new exhaust soon.
26.07.2012 Oil & filter change. MOT
passed at 81,015 miles. Still cannot find the source of the knocking noise. All
in the engine bay appears to be fixed firmly. The photos at left show the car on
The Moor, Sheffield and Locke Park in Barnsley.
12.08.2012 The 35 amp (3,4) fuse blows three times in
12 hours. Suspicion falls on the flasher unit and the brake light circuits,
possibly a wire shorting out somewhere.
15.08.2012 Circuits tested by my local auto-electrician
but no fault found. A 10 amp fuse was inserted at the brake light switch in
order to isolate this circuit and to see if this is the problem.
26.08.2012 The fuse continues to fail and even though
the brake light switch fuse is intact, the brake lights also fail
30.08.2012 All circuits on the 'ignition side' now have
10 amp fuses. Testing again proved fruitless but it was noticed the washer
bottle pump leads were touching the bodywork. As this too is on the 'ignition
side' it may have been shorting out and causing the whole circuit to fail. To
continue the saga, the circuits again fail when driving so I decided to purchase
replacement flasher and temperature sender units. When installing the
temperature sender, I noticed the wire from it was resting on the cylinder head.
With the washer bottle and temperature leads well 'out of the way' it was time
for another drive around and, for the moment, all seems well - apart from the
fact that the coolant temperature is now much higher than it should be! This did
not stop me from attending Rotherham Show and the village gala at Harley (photos
right).
Nope, the electrical fault remains. Need to pause and have a think!!!
March 2013 Purchased a few items from Earlpart ready
to fit next month - brake hoses and thermostat amongst others.
22.04.2013 I decided to replace the ignition
switch in an effort to rectify the electrical fault described previously.
Excellent service from Tim Hodgekiss of
Vintage Motor Spares (based in
Norfolk) who supplied the correct part at reasonable cost - Lucas 47SA.
24.04.2013 The car starts first time after being laid
up since October last, but the electrical fault remains.
13.05.2013 So it is back to the auto-electricians where
it was found that the main wire supplying the power to most of the electrics had
a spade connection which was corroded and was held together by only a couple of
strands of wire! This was removed (i.e., fell off) and the joint was soldered
together. Initial driving for a reasonable period produces no fault. It was
always going to be a simple problem to fix, but it took almost 12 months to
find! Because of this I put back the original ignition switch (to keep the new
as a spare) to cut down the number of keys on the fob.
20.05.2013 Sent the car to Wilsons of Cudworth to replace
brake hoses, thermostat, flush the radiator and have a general 'look see'. There
are some areas of corrosion which will need attention, i.e., the right front
corner of the driver's footwell and the 'trumpet' inside the right front wing.
The thermostat replacement and radiator flush were carried out because the
engine was getting hot.
01.06.2013 Attended the Rossington Vintage Vehicle
Rally near Doncaser which was a very good show and well attended for a Saturday.
The car managed reasonably well but the exhaust seems to be 'blowing' a little
and the rattle emanating from the 'engine bay' is getting annoying. I have
searched for the cause of this for quite some time, but cannot find it.
05.06.2013 The welding described above was
attended to at SJ Autowelding of Barnsley along with a crack in the exhaust. No
more 'blowing'.
08.06.2013 Despite the above problems, the car won only it's
second trophy at Braithwell Church & Country Fair twix Rotherham & Doncaster.
Most satisfying.
12.06.2013 Engine still getting hot despite a new
temperature sender and thermostat so the radiator was re-cored.
The old radiator
(left, which was not in too bad a condition) had 3 small rows of cores whereas the new has 2 larger rows to
allow coolant to circulate more freely. After a few 'drives' of over an hour
each, I am not convinced the recent work has cured the problem of excessive
water temperature.
It looks like the crankcase breather hose, when hot, is becoming soft and needs
replacement.
02.07.2013 The breather hose is replaced, but the hose
supplied is too short, so an extension is fashioned using a spare piece of hose
and metal tubing.
The joint of the left wing to bumper rail has had paint bubbling in the recent
past. This was refurbished today at D&S Motors in Mapplewell, Barnsley and the
whole of the bumper rail repainted.
03.07.2013 The heater motor has not been working for the past
few weeks so it was stripped down and found to be in good overall condition
except for a little 'blacking' on the commutator. This was cleaned and the motor
is back in working order. Removing the motor from under the parcel shelf is very
'fiddly' and twice as 'fiddly' to get it back in! Rear brakes sticking on when
hot.
The high temperature of the engine is getting frustrating - is it a blockage, an
air lock, the water pump or a blockage in the heater matrix? Or is it, perhaps,
simply the excessive ambient temperature?
06.08.2013 All 3 rear brake hoses replaced. The the middle
hose attached to the subframe was found to be partially blocked causing the
brakes to 'stick on'. Wheel cylinders & brake shoes in good order. Duct tape
applied around radiator until a proper radiator 'skirt' can be found or
fashioned.
Time to renew the brake hoses (far left).
Improvised radiator skirt (left).
March 2014 The car has
been under wraps for a little while, but, as usual, it starts first time. On
idling, the engine, however, continues to get excessively hot.
08.04.2014 Taken to the garage for a new water pump
and head gasket test. This found the head gasket had failed between
cylinders 2 & 3 yet again (3rd gasket in my ownership). Gasket replaced & a new
fan belt fitted.
04.05.2014 On the way to an event the car breaks down.
Whilst driving along, the engine begins to 'miss' a little, then stalls. Nothing
obvious under the bonnet so need to call the the breakdown club who diagnose a
faulty fuel pump. The car is eventually recovered home to await replacement
parts.
12.05.2014 A new fuel pump purchased and the car is taken for
it's fitting. However, the fuel line from the tank to the pump is too short to
enable the pump to be fitted and had to be replaced. A fuel leak was detected
and a hole discovered in the pipe fitting at the fuel tank end. This remedied,
the car refuses to start. Now it has no spark! The plugs, contact points,
condenser and air filter were changed. The engine fires up, but is running
'rough'. Time to reset the carburettor which cures the problem but the engine is
probably running a bit 'weak'. There is also some 'blowing' on driving. The
exhaust to manifold joint is re-sealed - some improvement. I feel the manifold
to cylinder head gasket may be faulty. Time will tell.
18.05.2014 Oil (20/50) and filter changed
following engine flush. Idle speed on carburettor increased and mixture
enriched.
20.05.2014 Carburettor found to be 'out' still - reset,
but now the distributor back plate is faulty and the spring keeps jumping out. The ignition timing was set, but
after a short drive, was found to be about 10 degrees out. A recommendation of
replacing the distributor with an electronic one was advised.
27.05.2014
Having
purchased an electronic distributor and coil from A-Series Spares of Ilkeston,
Derbyshire, they were fitted for me at Bell Lane Garage. As the more recently
manufactured coils are only filled with oil to 7/8ths of their capacity it is
prudent to fit them in an upright position. To fit them horizontally would mean
that part of the coil would not be covered by the oil. As usual with the older
cars, nothing is straightforward. My old coil was horizontal and, therefore, a
new bracket had to be made for it to sit upright. This was achieved by rotating
the existing bracket and adding a plate and drilling a couple of holes for the
new coil to fit. After a bit of coughing and spluttering and putting the HT
leads in the right order, the car fired up and ran fairly smoothly. The engine
is running a little fast so the idle speed is reduced to a satisfactory level.
Thanks to Keith at Bell Lane Garage for his help and knowledge of 'what goes
where'.
Below: The dynamo/coil strap 'A' was rotated 90 degrees, allowing bracket
'B' to be fitted. The coil will have to be removed to enable removal of the oil
filter housing 'C'. New electronic distributor 'D'.
It looks as though someone has backed into the car at some point. The offside
corner of the front wing near the bumper is cracked as is the perspex covering
of the number plate.
June 2014 A number of shows attended during June
and the car seems to be coping fairly well. Perhaps the engine revs are a little
fast on idle when hot. Should I leave alone or have a tinker?
12.08.2014 MOT failure due to corrosion to nearside
rear area under the car near the subframe.
15.08.2014 Welding to above area and to hole in offside
sill at the front - all undersealed. The cracked number plate is replaced.
18.08.2014 MOT passed, but, on entering details into the MOT
computer system, the car is only recognised as a Rover! A journey to the local
VOSA area office in Sheffield is in order and the details are corrected without
too much fuss - its a Vanden Plas again!