A chronological account of
living with the car & exhibiting at various rallies
Click here to see other Vanden Plas/Princess related vehicles
Introduction
Engineered by Alec Issigonis and designed by
Pininfarina, the Vanden Plas Princess 1100/1300 was the highest specification of
the Austin/Morris marque developed under the code name ADO16 as the range of
badge engineered cars which included the Riley, Wolseley and MG names as well as
the Austin, Morris and the Vanden Plas. It was the heir to the legendary Mini
and was a highly successful model during the time of it's production from 1962
to 1974. During the sixties, the range of 'ADO16s' outsold all other cars save
for one year when the Ford Cortina became 'top dog'. Of the 2.25 million
produced, about 43,700 units were the
Vanden Plas derivation. There are still many examples on the road
today despite the issues of 'build quality' surrounding British Leyland at the
time. This is testament to their owners rather than the manufacturer.
The name -Vanden Plas- is always pronounced as it reads and never as 'Vanden Plah' and is of Dutch origin possibly meaning 'of the pond' (to be completely correct, Van Der Plas). The company, Carrosserie Vanden Plas, originated in Brussels, Belgium in 1870 as a wheel manufacturer for the carriage trade (VPOC). It first appeared in England in 1906 and from 1923 their coach-building production was based at Kingsbury (formerly Kingsbury Aviation) in London until its demise in 1979. The title 'Princess' ( in association with the name Vanden Plas) was dropped in about 1974 when the 11/1300 variants were discontinued, although the name 'Princess' was used by British Leyland on its own (as in the BL Princess 'wedgie'). The name of Vanden Plas continued with various models such as the Allegro, Montego, Metro, Rover, etc, and today is borne by 'top-end' Jaguars and Daimlers. YDT ***G was one of those born at Kingsbury in 1969 and the car has only recently passed its 39th birthday (March 2008).
General Specification
A front
wheel drive, four door
saloon with an ‘A’ series transverse BMC engine of 1275cc, 4 cylinders, OHV with a single SU
HS4 carburettor, the
engine giving approximately 65bhp. This example is fitted with the hardy,
but unsophisticated AP automatic gearbox. Top speed is 80-90mph with a 0-60mph time
of 18-22 seconds. This
particular car has had an unleaded head conversion and returns an
economy of 30-35mpg from it's 8 gallon fuel tank. Front disc and rear drum
brakes slowly curtail forward momentum as there is no servo-assistance. It has a turning circle of 34 feet 9 inches and is 12
volt negative earth. Dimensions; length 12ft 2in, width 5ft, height 4ft 6in;
wheelbase 7ft 10in; ground clearance 6in; weight 1904 lbs (864kg). Which is
just under 1 ton.
Brief history of YDT***G
Purchase
price in 1969: £874 + purchase tax = £1,143. Built 6th to 10th
March 1969.
Dispatched 24th March 1969 to E.W. Jackson and Son
Limited of Doncaster. First registered 3rd April 1969 and issued in
Doncaster as YDT ***G.
Assumed to have been purchased by a gentleman from new
probably in Doncaster. Passed to his niece in Goole for a short period. Purchased
by 3rd owner from Doncaster 19th March 1993 having
covered 33,951 miles. Kept in excellent condition regardless of cost throughout
ownership and a regular feature of the classic car scene for many years
supporting the local ‘Traditional Car Club of Doncaster’. Purchased by me 17th
December 2004, being the 4th owner having covered 62,465 miles.
Colour: Sherwood Green with Champagne Beige part leather seats and armrests and
the interior is trimmed with
Walnut veneered wooden fascia and door cappings, the front seats have fold down picnic tables
for the comfort of rear seat passengers. Below is the authentification
certificate from the British Motor Industry Heritage Trust,
click to enlarge.
02.04.1993 Non standard radio & accessories.
10.04.1993 Wing
mirrors
09.06.1993 Black
& silver registration plates
17.07.1996 Exhaust replaced
26.09.1999
Radiator replaced
15.09.2000
Torque converter replaced
14.12.2000
Unleaded head conversion
19.10.2002
Recored radiator
12.11.2002
Engine mounts replaced
22.07.2003 Fuel
pump replaced
08.08.2003
Exhaust replaced
03.07.2004 Waxoyl check
A chronological history since my purchase
17.12.2004 Clock inoperative, headlight beam
?misaligned, speedometer needs checking for accuracy, ?vibration to steering wheel, locate
trip counter reset, flasher warning light ?inoperative, ashtray handle loose,
decide if alternator should replace dynamo.
18.12.2004 Draper battery conditioner
purchased with 3 x 1 amp glass fuses.
19.12.2004 BMC Service Parts List (c1968) for
1100 & 1300 models, Newark jumble. Flasher warning light operates. Headlight
beam appears ok when lights shone against suitable background, on driving, left
beam seems ‘lower’ than right. Noticed black marks on carpets to front passenger
side – to investigate. To check brake fluid and brake cylinders.
11.02.2005
Intermediate service requesting
to change oil, investigate oil leak, change oil & air filter and plugs. To drain
and replace brake fluid with DOT4 and check cylinders, pads and shoes. To advise
re; clock inoperation, trip counter reset mechanism, underbody & waxoyl
protection, subframe mountings, exhaust, ?excessive cabin engine noise and
varnish ‘lifting’ to door cappings. Found slight movement in o/s gearbox drive
flange (probably the cause of movement/vibration to steering wheel). Oil leak found to be
from filter bowl, seal and new filter fitted. Oil drained and refilled. Plugs
changed to NGK BP6ES. Air filter okay. Anti-freeze okay to -15 degrees. Wheels
removed, front calipers and pads okay. Rear cylinders and drums okay. Brake
fluid drained and refilled, system bled. Suspension trim height found to be down
by ½”,
suspension blown up to required height. Clock inoperative, may need dash off, could be
US as it should be disconnected if not working. Underseal required to small area
at front of car. Subframe mountings okay as is exhaust and engine noise. To
further enquire about varnish lifting.
11.03.2005 Rear left brake needs ‘taking up’.
Need a proper hub cap remover. To feed leather with hide food.
18.04.2005 To garage for: Tightening of drive
shaft flange, underseal to front of car, taking up of rear left brake.
04.05.2005 Connolly Hide Food to seat backs,
not squabs, except drivers seat. Badges to badge bar, YTCC & TCCD to bar and RAC to grill.
Advice from mechanic, car is definitely negative earth.
22.05.2005 Oil filter & plugs from Newark.
Previously, brake pads & shoes.
30.05.2005 To look for Fogranger surrounds.
Drivers door checkstrap for repair. Check headlight alignment. Door capping varnish.
09.07.2005 Returning from
West Stockwith,
Lincolnshire, advised of a split in front right tyre. Noticed bulge to tyre. Wheel
changed. Later painted wheel and noticed tyre was remould but with plenty of
tread.
11.07.2005 145R12 tyre from
local tyre centre, suggesting the cause was a pothole breaking the cords. Wax
polish (paste) to roof, bonnet, front wings & bootlid. Used Turtlewax. NECPWA
badge to badge bar.
12.07.2005 Chrome tailpipe 35mm (13/8”)
from local motor factor. Engine does not sound ‘right’ & is getting a little hot
when idling. To look at the plugs, carburettors.
14.07.2005 Exhaust may need a new clamp at
the manifold to front pipe joint, but this is unclear. Possibility of fitting an
extra fan for the radiator by fitting a bracket to the inner wing. Underside of
car looks good, most rubber mountings appear in good condition. Window scratches
to be polished out.
Tin
of ‘2 pack’ BLMC Sherwood Green paint from local paint supplier. From their
experienced eye there is a mixture of colours around the car. The gold
coachline has not been continued fully to it’s proper length. For a full respray
at some point (will require c£100 of materials).
Whilst trying to secure hubcap centre pieces, all metal securing tags broke off.
Changed hubcaps to ‘solid’ chrome ones for now. Immediate jobs to do, therefore;
Replace; Hubcap (& centres), rear view mirror. Paint; Bonnet marks near
bulkhead. Bulkhead in engine bay. Clean; Front valance, tyres, wheels, hubcaps.
Buy; Hose bandage for badge bar protection. Fan belt.
16.07.2005 Whilst returning from a show at
Ackworth, right rear hubcap fell off and was run over by another vehicle and
distorted (RIP!). Both rear wheels fitted with original hubcaps (the best of the
3) whilst the front continues with the solid.
31.07.2005 Black plastic wiper arms & blades
x2, Lucas rotor arm, Lucas contact points, Fogranger x2,
hubcap with centres x2. All from autojumble at 1100 club rally at Rufford
08.08.2005 Full service & MOT.
Oil changed to
20w/50, filter replaced. Engine tuned a little to prevent ‘run on’. Driver’s
door check link not repairable without removing door skin; the link is broken
and it’s fixing point is riveted to the skin via a box. Exhaust manifold to
front pipe joint sealed to stop exhaust ‘blowing’. Window scratches probably
caused by window rubber being too hard. Plugs, condenser, contact points, rotor
arm renewed. Wipers renewed with black plastic ones to pass the MOT. Bonnet
moved forward to clear ‘bulkhead’. Exhaust tailpipe finisher screw missing. Engine
mountings, corrosion and underseal check carried out last week. Headlight
alignment not done. Hubcap centres fixed to hubcaps by using jubilee clips
(holding rubber centres to hubcap centres on inside). MOT passed – runs from 20th
August. At 64,500 miles. Air filter purchased.
16.08.2005 Cleaned
Fogranger spot lamps
purchased at Rufford with Autosol. Cleaned and fixed hubcaps and centres to
front wheels. Need self tapping screws for exhaust tailpipe finisher.
20.08.2005 Exhaust tailpipe finisher
replaced. Found front passenger door window seal to be split whilst using
Autoglym Bumper Care (to clean rubber and to keep it soft). Used Hamilton's
Leather Cleaner on rear seat and front passenger seat for first time – can’t see
much difference. Cleaned dash with Mr Sheen (he didn't mind) – looks ok. Found some
scratches on
front left wing, attempted to T-Cut them out with little success. Removed
steering wheel cover to reveal it’s perfectly adequate condition.
Photos prior to painting - click to enlarge
2.11.2005 Car sent for painting & for odd
jobs. To paint both front wings (bubbles noticed under both headlights), passenger
side rear door, rear panel, bonnet scuttle area, touch up engine bay under brake
fluid reservoir. Repair driver’s door checkstrap. Replace fog lamps with
supplied. Powder coating to 5 wheels. Waxoyl all cavities. Photo record of
problems/work done. Right headlight bowl found to be corroded - replaced.
Select this link here to see photos of the painting process. Images courtesy of M.Wootton.
18.01.2006 Painting done as described 2.11.05. Wheels powder coated by a firm in Castleford. Waxoyl all round. New aerial supplied as old one US. Driver’s door checkstrap partially repaired as part of the fixing was broken on the door itself.
21.04.2006
Began to run car after lengthy time in
garage. No real problems.
28.04.2006 Oil change
at 65,000 miles. New rear
exhaust mountings.
01.05.2006 35 amp fuse in
the 3-4 position in
the fuse box blew twice on the way to a show. Fuse box needed cleaning and bringing up
to scratch. Purchased extra fuses and second hand fuse box at Thoresby autojumble.
Head gasket set also bought.
03.05.2006
Replaced fuse box after thorough cleaning. Cleaned most electrical terminals.
Removed battery, repainted battery tray and cleaned terminals.
04.05.2006 Repainted
air cleaner gloss black
to cover previous overspray. Cleaned rocker cover satisfactorily of overspray –
still some in engine bay.
06.05.2006 16x 35amp fuses from Ackworth
jumble.
11.06.2006 Wheel and tyre purchased as spare.
29.06.2006 Attempted to refurbish side/flasher
lamp cluster without success. Rubber seals in very poor condition. Sidelight terminals cleaned. To look for Lucas
L746.
12.07.2006 Requirements: Rubber seals for
flasher units; Hubcaps with centres, Hubcap remover,
Interior mirror, Door cappings, Exhaust clamp, Fuse box.
16.07.2006 1100 and 1300 BMC Workshop Manual
from Newby autojumble.
17.07.2006 Arranged for MOT w/c 20.08.2006. To
check underbody, passenger front door ?sagging.
22.07.2006 Cleaned and painted coil and
bracket. Took all afternoon to remove the ‘elbow’ (top hose to thermostat) for
cleaning. Managed to remove interior mirror and discover how it is fixed – to
enable replacement as the old mirror is ‘yellowing’. The opportunity was taken
to remove the rocker cover and to inspect the gasket. The gasket was in good
condition. The rocker cover was found to have some of the chrome peeling off in
2 or 3 places. The cover and fittings were cleaned and polished before
replacement. The rocker shafts and arms looked clean and well oiled.
28.07.2006 Leather paint in ‘Biscuit’ from
Frosts.
29.07.2006 4Life from Holden's, fuse box to
follow. I am informed that 4Life coolant does not need replacement but just
topping up.
14.08.2006 Fuse box from
Holden's.
27.08.2006 Whilst driving to Crich Museum,
engine sounds a little rough. Possibly exhaust blowing. Discussion with YTCC
member suggests ‘pinking’ although I am not convinced.
05.09.2006 Exhaust manifold
gasket blowing.
Awaiting replacement. Hubcaps need replacement.
09.09.2006 Received car back after above gasket
& tuning.
10.09.2006 To Otley & back with no problems.
24.09.2006 Top radiator hose, rotor arm and
Desmo badge clip from Newark autojumble. Engine noise returns but cannot
pinpoint the cause.
01.10.2006 Inner wing to subframe mounting
(need another for the set), interior mirror (subsequently broke) from York
autojumble.
04.10.2006 Suspect head gasket problem as I
can feel blowing from rear left side of head or manifold. Car taken to the
'menders' where the diagnosis is confirmed – the head gasket has gone! Luckily,
I have a spare set.
12.12.2006 The car has been unused for some time now. Didn't really want to start.
11.01.2007 Tried it again! No problems!
Is there a problem! Seems to run okay for no particular reason. Ah well, if it's
not broke...
21.01.2007 Bought a few service items from
Huddersfield Autojumble - oil filter, brake pads, rotor arm, engine and subframe
mounts. On 27th February at Huddersfield, bought a further rear view mirror and
a head gasket set as a spare.
30.03.2007 Car sent for 'pre-season fettling'. The
battery was checked and found to be okay. The engine was again running hot and
sounding as though it was 'blowing' a tad. A little grinding to the exhaust
manifold, a new gasket and a new exhaust system was required and the engine
tuned which eliminated the above problems. Now sounds sweeter. Front passenger
door lifted to ensure good closure. Points and plugs cleaned. Oil and filter
changed. Underside of car treated as required with sealant. Suspension height
reset. The car needs a run to ensure the above have improved things to the
necessary standard. Current mileage 67,850.
17.04.2007 Collected the car and went for a short run
which presented no problems. Fitted the new rear view mirror without breaking
it!
22.04.2007 Attended Elsecar Heritage Centre near
Barnsley as part of the FBHVCs recommended 'Drive It Day' run by the Traditional
Car Club of Doncaster (TCCD). A very good turn out of cars with over 150 present.
Talbot, Vanden Plas, Daimler SP250 and Porsche 356 - just a snippet from the
car show. The Talbot and Daimler were my 'cars of the show', see 'Classic Shows'
page.
22.05.2007 No problems with the 'Princess', but idle speed of the engine probably needs advancing a little. After almost a week of rain today's weather was exceptional and the Traditional Car Club of Doncaster's event at the newly renovated Cusworth Hall was an outstanding success with over 240 cars attending their 'Picnic in the Park' with the added attraction of the 'Battle of Britain Memorial Flight' flypast in celebration of the 50th anniversary of the flight's inauguration.
Just a few of the attractions at Cusworth Hall near Doncaster, more pictures on
the 'Classic Shows' page.
28.05.2007 Unfortunately, bad weather
prevented me from attending Nostell Priory near Wakefield for their Steam and Country
Show as I had planned.
03.06.2007 The Pre-War Austin 7 Club
must be congratulated for putting on an excellent show at Wollaton Park, Notts.
and for providing the good weather. It was a drive of over an hour to the venue
and the Princess coped fairly well, the engine only getting warm whilst queuing
to get in. Besides the vast array of Austin 7s of all shapes and sizes, there
were many varied vehicles from all periods including some commercials, buses and
modern day models. In addition there was a large autojumble, brass bands and
craft stalls to cater for most tastes. All in all, a very good day out.
I have noticed some minor signs of rust along the passenger side of the floor
pan where it meets the sill which will need attention at the end of the
'season'.
30.06.2007
Unfortunately, the 'weatherman' again intervened and prevented me from attending
the Waddington Air Show.
01.07.2007
Determined to attend one
show this weekend, I went to the Clumber Park Steam Rally and Country Fair. The
car performed favourably but was quite dirty by the end of the day. The weather
was changeable in the extreme, heavy showers and bright sunshine, the ground
being sodden. Did not particularly enjoy it!
15.07.2007
The
Newby Hall show near
Ripon once again did not fail to please despite the weather - a very wet drive
home, loads of spray! Cleaning the car revealed more areas that needed
attention, eg. overriders probably need rechroming at some point, some paint
peeling on
wheel arches, front passenger seat is a little askew and needs twisting (?) to
allow the picnic table to seat properly.
22.07.2007 My intention to exhibit the
Princess at the Ackworth Steam Rally was thwarted at the entrance by about 6
inches of mud! So I turned around, consulted my diary & found the East Yorkshire
Thoroughbred Club was hosting an event at the Elvington Air Museum near York
which turned out to be quite enjoyable except for one prolonged shower, but once
it passed there was warm sunshine. Plenty of classics and air exhibits. No
hiccoughs from the car on the drive there or on return.
28.07.2007 Purchased a pair of second-hand L746 sidelight units
without the original rubber seals.
29.07.2007 A 50 mile trip to the 'Traditional Car
Club's' event at Rufford Park near Ollerton (Notts) did not suit the car. An
unknown noise was heard towards the end of the drive down, a noise which did not
sound too healthy. Switching off the engine and moving the key to the 1st
position saw the temperature gauge soar immediately to 'hot'.
There also seems
to have been too much pressure in the cooling system as the top hose was quite
hard. After allowing the engine to cool, the radiator needed topping up and the
expansion tank was empty. The noise ( a whining sound) has yet to be identified,
but I think it needs to go the menders! My thanks are due to those who offered
advice and assistance in trying to solve this 'headache'.
The show itself was very good with a number of members cars, the added
attractions of a craft fair, dog show and the facilities at Rufford, made for an
enjoyable experience.
08.08.2007
Diagnostics revealed that the ‘whining’ noise
experienced during my journey to Rufford emanated from the dynamo (never thought
of that one). Apparently the bearings in the dynamo were excessively worn and
beyond salvation. A replacement was, therefore, sought and fitted. It seems the
coolant problems were a ‘red herring’. The high pressure in the system is normal
after a long run and when the engine is hot but the radiator expansion tank
should not have been empty. It should, however, be only a third full. I
over-filled it when found empty as I found out when I released the radiator cap
on reaching home – coolant everywhere. Fortunately, I had allowed it to cool
down beforehand. The apparent over-heating could also be explained away. If you
switch off the engine when it is hot and then turn the ignition key to the 1st
position, the temperature gauge will continue to rise until the engine has
cooled. It follows that when the engine is not turning over it is not driving
the fan and, therefore, allows for ineffective cooling. On top of this, if the
dynamo is defective, it may not drive the fan at the correct speed.
19.08.2007 Attended the 40th Anniversary Show of the
Traditional Car Club in Doncaster. A rather showery day spoiled what was
otherwise a very good show and included many attractions which was topped by a
flypast of a WWII Lancaster bomber.
21.08.2007 The car fails the MOT on handbrake efficiency
which was later attended to. The retest was successful, but the handbrake now only
moves 'one click' and is difficult to release. What a ridiculous thing the MOT
is where firstly, a retest is required once a particular problem is eliminated
and, secondly, it states that the certificate is not evidence the vehicle is in
a satisfactory condition! What is its purpose in that case?
22.09.2007 A 50 mile (or so) drive to a
show in Gainsborough, Lincolnshire, did the car no good. On reaching the show
field I noticed fluid on the rear offside wheel and tyre and, on wiping it off, I
found the wheel to be extraordinarily hot! At first I thought it was oil, but
further investigation revealed it was grease and my thoughts turn to a wheel bearing
problem. So as not to compound the problem, I decide to have the car transported
home and contacted the RAC to do the job. Whilst I have had no real problems
with them before, today proved somewhat different. One and a half hours to wait
for assistance - a van was sent to diagnose the problem - an hour later, the transporter arrived, but it was the wrong sort. It was a '2 wheel lifter'. You
cannot lift an automatic to run on the driving wheels. A little later, the right
one appeared and 4 hours after the 1st call, I arrive home! My planned trip to
the Beamish Museum tomorrow is scuppered.
25.09.2007 The car is sent to the garage for diagnosis
& fixing. On it's return it appears the brakes were over-adjusted at the
last MOT and were binding causing the area to get hot which melted the bearing
grease. Fortunately, the bearings were in good order and nothing further was
required after re-adjustment of the brakes.
06.10.2007 A long run to Sturton in
Lincolnshire proved to be uneventful - no problems with the brakes. A bonus was
2nd prize in the Classic Car Section of the Sturton by Stow Agricultural Show
run by the 'Lincs & Louth Motor Club'. This is the 1st time an award has been
achieved during my ownership.
An even longer run the following day to a show at Bolton Abbey Station, North
Yorkshire, again proved uneventful for the car.
03.11.2007 New spark plugs fitted,
NGK6BPES, contact points examined and seem okay.
22.01.2008 Rimbellishers, hubcaps and
overriders sent for re-chroming as they are looking decidedly tatty.
04.03.2008 The above chromework
collected from Prestige Electro Plating of Mexborough, South Yorkshire who have done quite a good job. The
re-fitting will have to wait as the car is presently undergoing a pre-season
examination.
01.04.2008 Enquiries to my 'fettler'
reveal the passenger side footwell needed welding and the front passenger seat
requires further examination to enable it to 'sit right'.
18.04.2008 At 69,770 miles the following has been
undertaken; oil flush, oil and filter change, throttle cable lubricated and a
clip for a cable under the nearside front wing to prevent trailing wires is
contrived. Welding was required to the front passenger floor panel and inner
sill and a plate to the underside of the floor pan to the sill with primer
applied.
20.04.2008 Today is 'Drive It Day', so I drove it....to
Elsecar Heritage Centre where the TCCD was holding a rally. Unfortunately, the
weather was unkind, cold and wet, which encouraged me to leave earlier than I
normally would have.
27.04.2008 Oh dear! Another show and more rain, this
time at Tadcaster which is, nevertheless, fairly well attended. The car has
exhibited no problems whilst attending these shows despite the lengthy winter
lay off.
18.05.2008 An early start to attend a
show at Sewerby Park in Bridlington, North Yorkshire. Not having attended
before, I did not realise it was so far, taking 2 hours to get there. The show
itself was organised by the East Yorkshire Thoroughbred Car Club and was very
well attended. Only a cold breeze detracted from a sunny day. Sewerby Hall
itself is by the sea and makes the venue all the more attractive. A few miles
further brings you to Flamborough Head and it's lighthouse - picturesque. The
only downside was the distance I travelled of 156 miles - 4 hours on the road
takes it out of you! The top speed of 60-65mph was handled admirably by the car,
no stuttering at all.
Images L-R from Sewerby, Nostell, Cusworth, Sherburn,
Wollaton, Brodsworth & Sledmere - click to enlarge
24.05.2008 Attended the Nostell Priory Steam event near
Pontefract. The car appears to be running okay but a rattle from underneath is
bothersome and seems to be getting worse. My mind turns to the exhaust which is,
however, only a year old. The show was reasonable, the day sunny but the wind
made it a little chilly.
25.05.2008 Today brought a 'Picnic in the Park' at
Cusworth Hall near Doncaster, a very well attended event on a sunny but very
windy day.
26.05.2008 The third show in 3 days when I turned up at
Sherburn Aero Club's Vintage & Veterans Day at Sherburn-in-Elmet, Yorkshire. The
wind persists and I am surprised to see aerobatics taking place despite
this. They don't usually fly sideways do they? An excellent bacon sandwich and a
good display of cars and aircraft did not dampen the spirits.
01.06.2008 Another early start to go to
the 'Autokana' at Wollaton Park, Nottingham. Rain and spray on the motorway made
it a filthy drive down. It continues rain to mid-morning and then it was just
'grey' but, thankfully, not as windy. It would have been an excellent show but
for the weather. The rattle under the car is worse.
04.06.2008 Can't stand the rattle any more so it's off
to the menders! I also discover, whilst driving in the rain, the driver's side
demister vent seems to be blocked.
14.06.2008 A metal disc was removed from the inside of
the exhaust which was the probable cause of the rattle. A drive tomorrow will
give proof. It seems that the near-side sill has previously been replaced but
the end was not sealed thus allowing water to collect in the area when draining
from the roof gutter and down the A post. This was patched and may require
removal of the wing to facilitate a proper repair. The heater/demister vent on
the dash rail was cleared. On it's return I treated the car to a new battery as
the old one was on it's last legs.
15.06.2008 Visited Brodsworth Hall near Doncaster for a
'Fathers Day Classic Show'. Mostly warm with one heavy shower. A good show. The
rattle under the car has mostly disappeared, but is still evident when going
over bumps in the road.
29.06.2008 A 69 mile trip to a show at Sledmere near
Driffield returned a figure of about 34 mpg and, at around 60-65 mph, in these
days of high fuel prices is a number I can live with. This does not, however,
mean I should not try to get more by driving more economically. The show itself
was, as usual with NECPWA, very good and the setting of Sledmere House very
pleasant. Spots of rain in the early afternoon saw people heading for the exit
so I decided I would follow. Shortly after the heavens opened and the drive home
was unpleasant. The car took it in it's stride with no problems at all.
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